D318MKN
This GT/e coupe was bought after being stood for almost 2 years. A previous owner had done a lot of work cleaning and rebuilding the engine and suspension, fitting many new parts before finding out the chassis needed welding. He sold it on and the next owner handed it over to be fixed at a specialist MG restorer local to him. They then spent over a year trying to find all new replacement panels before starting the work (chassis rails and floor pans). The owner finaly had enough of waiting and sold the car on again. Which is where i came in, i collected the car from near Burnely and trailered it home to start the rebuild. The front end had rot in the nosecone, floor and chassis rails but the sills and rear were in good condition. It took quite a while to repair as i had to completly strip the front end for the chassis rail repairs. Once done i sold the car to a friend (after much
begging on his part) and he enjoyed it for a year. Then a dozy old lady
in a Ford C-max pulled out infront of him on a dual carridgeway and
shortened the front end a bit. The insurance company wrote the car off as it was behind economical repair. Happily he managed to buy the car back as salvage and still get a good payout. So after another trip to collect it, the car once more returned to my garage for some TLC Once more the car is back on the road, we have some future plans for it but i need more garage space before i can do yet another rebuild. (click pics for larger images) |
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How the car looked when first purchased
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The front carpets had been removed
to check the floors
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Chassis rail and jacing point had
been left exposed
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Battery tray holed
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NS chassis-leg previously badly repaired
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OS chassis-leg gone completely
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OS chassis leg under floor looking
bad aswell
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OS A-pillar holed, as was washer tray
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Strpped car in garage
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NS chassis leg chopped out
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Rebuilding OS chassis rail
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NS chassis leg going in
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Outside of NS leg
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Undersealed and suspension back in
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Battery tray minus holes
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Rolled out for the dust to be blown/washed
off
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Less
than a year later it had a close encounter with a C-Max
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Written off by the insurance but bought
back as salvage
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Wing and nosecone off to expose the
damage
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Bent inner front panel and radiator
tower off to help the repair
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Hyd body press used to re-align everything
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Rest of nosecone removed
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Replacement nosecone, wing and bonnet
sourced from Sean in sussex
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Nosecone clamped in place to check
alignment
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Pile of junk bits removed during repair
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Now sold to Sean as his 2nd car on the road replacing his tatty and problem riddled 1.8 hatch. |
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All
finished and back on the road.
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